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<s>[INST] Product Notice 2009-04-001 and 2009-04-002 - PowerFlex 700 Regarding Product Notice 2009-04-001 and 2009-04-002 - PowerFlex 700 NEMA 12 AC Drives: I purchased on 2/1/2008 a powerflex 700 drive PN: 20BD292A3ANNNNC0. I read the article in the knowledge base, and did not the drive listed as having the fan defect mentioned in the product notice. Can you confirm whether or not this drive has the fan defect? If so what is the replacement kit part number? [/INST] For the Product Notices you mentioned, your drive is not listed to have this problem, so you shouldn't be worry about that. :smileyhappy: - fuzzy logic \\n </s> |
<s>[INST] 1756-M08SE - Sercos Ring State with Kinetix 6000 Servo's Hi There, I am adding a new axis to a customers existing system. I came across a MSG instruction that appears to be reading the Sercos Ring state of the Sercos Card. Personally I've usually used the Axis.SercosRingFault bit for each drive. But this message instruction has me curious. I've downloaded and reviewed all the Sercos and Kinetix 6000 manuals I can find and none of them reference using a MSG instruction. Attached is the Rung with the Message configuration, the Path just points to the Sercos Card on the backplane. Can anyone here point me to the right manual so I can see what this is doing/reading? Regards, Vin [/INST] That message will request the current phase of the SERCOS network. See technote 26687. I'm not sure which manual this information could be found in. \\n </s> |
<s>[INST] PF700 datalink limitation? Summary: Why can't I transfer a value >18,000 to parameter 101 preset speed 1 via datalink? Hi, I am using a PowerFlex 700 drive 20BC015A0AYNANC0. I set Speed Ref A Sel = 11 in order to operate it in Preset Speed [/INST] Paul, try to read here: 55736 - Datalinks are limited by previous value of limiting parameter 56977 - Why is my linked reference parameter to a PowerFlex 700VC not matching the data output reference from the controller? - fuzzy logic In order to enhance the reputation of the Forum's contributors, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] PowerFlex 40 trips GFCI I have a 120v PowerFlex 40 that trips a GFCI when you press the start funtion. Works fine when on a non GFCI circuit. Whats causing the GFCI to trip? [/INST] This is quite normal, and usually it happens due to filtering...the filter works by filtering the noise down to earth which would cause the GFCI to trip. Follow the instructions in the User Manual, page 1-7, and use a Type B RCD Also take a look to the following technotes: Aid 40028 - Aid 40632 Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] PF700S Feed Source Summary: Use DC Bus or 3-phase AC power. Hi, Anyone knows the performance advantage if PF700S drive, feed from DC Bus versus 3-Phase AC power supply? PF700S will be use to control direct motor in torque mode. Thank you, [/INST] I don't really think this performance advantage is worh the required material investment. PF700S on-board DC power suppy is pretty capable and free when a drive is purchased; when properly observing the line/load requirements (isolation transformer or line reactor and the eventual load reactor) you will get pretty much a top tier torque/variable frequency system; an external DC power supply might be required for an extremely precise muti-drive system, however, more often than not, the VFD's DC Power Supply will do. \\n </s> |
<s>[INST] PF40 vs. PF40P Had some new equipment installed in our facility. It came with several PowerFlex 40 drives which we have many of in the plant. But, it also came with one PowerFlex 40P. Anyone have a very short list of the differences between the PF40 and the PF40P? Thanks. [/INST] Very short side-to-side compare is inside Selection Guide, pag.11 Otherwise, here more detailed infos for PF40 and PF40P Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] PF 70 ON COMMON DC BUS? HI ALLCAN PF 70 RUN ON COMMON DC BUS?DO WE HAVE DOCUMENTS FOR THIS?THNXS IN ADVANCE [/INST] PF70 has not DC bus terminals, therefore it cannot works with common dc bus.You may consider PF700. \\n </s> |
<s>[INST] I need the internal circuit diagram of the device kinetix 5500 Hello I live in Iran And due to international sanctions, I don't have access to authorized rockwell automation repair centers I have a kinetix 5500 model drive which encountered error s11 inv overtemp To repair this drive, I need the circuit diagram inside the drive Please help me? Is it possible to access the diagrams for me? [/INST] Hello Sheikh, If documentation is not available in the Rockwell Automation literature library, it probably is not available to the public. Do you have an accounts manager who could possibly help you out in this case? Literature Library Thanks \\n </s> |
<s>[INST] Load Sharing with 700H I have two 700H drives driving a single conveyor belt. The drives are running one motor each separated by about 4m.How do I set them up so that they both run together, sharing the load, without the risk of having one run away? The only control option is Open-loop Speed Regulator.If both drives are set up exactly the same and both get the same speed reference, will setting the Droop @FLA on one drive only really make it work? [/INST] PJWZA,I hope it should work as i guess the application is not that critical.Droop should work fine here.:smileywink: \\n </s> |
<s>[INST] Kinetix 6500 display error SAFE FLT 17 SMS SPEED Hello everyone, currently, i have big problem with Kinetix 6500, my device control 1 axis. The issue display on small LED is SMS 17. The description for this error is actual speed exceed setpoint speed. However when I access to Properties inside this Axis, i can not find any limit or condition on speed. Please help me to find location for limit of speed inside axis program. thanks [/INST] Hello nguyen Could you provide some more details . I mean what is the Kinetix reference that you are using and motor connected to it. it is clear that you are facing a Safe Maximum Speed motion fault. So in your application code you are asking the axis to run faster than the safe speed limit configured. So you will have 2 options : 1) understand what is that limit and run slower or 2) change the safe limite speed (dut that will impact the Machine Safety validation... so i would not recommend this 2nd point without more investigation and safety assessment plan ) So to check the value of the safe limited speed that have been set you have to connect to the drive webpage look at this manual : 2094-RM001C-EN-P Kinetix 6200 and Kinetix 6500 Safe Speed Monitoring Safety Reference Manual (rockwellautomation.com) once you found the limit you can trend your axis speed in logix and understand what is the issue . Best regards \\n </s> |
<s>[INST] How to compare online and offline project changes? How to compare onlinevproject and offline project. Today, I was online with PLC until lunchtime. After wgwn I try to online, I got a poup message to upload/download project. There is a change in online and offline project. How to know what changes or which routine or rung got changed before upload or download. [/INST] Upload a copy from the controller and save it, then use the Logix Designer Compare Tool. In the Compare Tool there also appears to be a Logix Definition Compare, which I think compares AOI definitions within the projects.\n </s> |
<s>[INST] Help for a Kinetix VPL motor I have a servo motor, VPL-B0631T-PJ12AA, which has a bad encoder. Is the encoder programmed specially for a certain size motor or will any encoder with the exact same sick model number work as a replacement? Thanks! [/INST] Hi Wesley Encoder replacement on a VPL motor can only be executed by a Rockwell Automation specialist. You need specific tools to aline the encoder to the motor shaft and Program the Digital DSL encoder. The encoder store multiple data, like motor serial number, offset, reference...etc. It is used for monitoring position, but not only, we also use the encoder to determine the shaft orientation relative to the coils... this is why all those operations require a specialist with specific equipment. So you have 2 options : replace the motor with a new one, or send your motor to the Rockwell Automation repair center. regards Vincent \\n </s> |
<s>[INST] Random noise faults I have a K2K/ControlLogix system with 7 1510V motors that I keep getting random and sporadic E64 and E07 faults jumping around on various axis. I have verified grounding, shielding and seperated the wiring as much as possible. There are no contactors or anything of the such that would be generating spikes and I've had a power analyzer put on the incoming power to ensure that there are no issues. I saw a tech note that certain motorshad issues with a 5V short in the encoders that would do this but these motors do not fall into that category. Help.......please? [/INST] Are the feedback cable connectors factory made at both ends, or have they been terminated into the big silver connectors by a panel builder? \\n </s> |
<s>[INST] 22-COMM-E Language Issues Summary: Language in Parameter List of 22-COMM-E not English and not settable Greetings, Has anyone else come across this issue? If so, what was your solution? I have experienced, along with my PLC guy, and a customer; that when connecting to the Comm Card and looking into the parameter list of the that comm card, the default language appears to be German, but is not changeable or Selectable. I was told that if I re-establish my database files in Logix that this will go away, but I have also experienced this in the 1203-USB using CCW V4.0, and I am not aware of any database file update for that. Again, if input to a resolution is greatly appreciated. [/INST] A possible solution: From CCW: - Create offline drive (whatever type) - Go to Properties - In upper right, click on button for Create device database... - browse to online drive. However, a warning is given that the software might reset the drive. \\n </s> |
<s>[INST] ultra 3000i E022 fault Summary: drive trips after running awhile.I have an Ultra 3000i indexer drive, will run quite a few cycles then trips E022. this just started on an existing system thats run fine for years. Motor is cold to the touch. no brake in motor. N-3412-2-H00AA. Mechanical gearing seems fine. no drag. Online with ultraware v 1.8 wont let me shut off software protection, as i figure its the default parameters for that motor. any ideas to prove drive,motor or mechanical is the issue??? or how to disable the software protection? [/INST] E022 is Motor Thermal Protection Fault, and it is apparently calculated. It is different than E04, which is motor overtemperature. E04 comes from the motor thermostat on pins R and S of the encoder cable. I do not think you can disable this fault. Are you sure the motion parameters have not changed recently? Did someone change the accel rate without your knowledge, or decrease the time of the move? You do say that it takes quite a few cycles before it trips. After the first fault, does the fault reoccur with increasing frequency? I would check power lead connections from drive to motor for tightness or thermal discoloring. \\n </s> |
<s>[INST] 700S Simulated Encoder Output Looking at an application where a motor mounted encoder needs to go to the 700S (for drive/motor loop closure) and an M02AE card. Sure, you can parallel the signal and put a buffer/repeater module in. What would be nicer is if the 700S had a simulated encoder output module, like a Control Techniques drive. Anyone know of an addon module for this purpse? [/INST] Try Motrona encoder splitter. \\n </s> |
<s>[INST] 825 P protectiection relay serial port connecting Summary: Problems connecting to the relay with the serail port I am trying to connect to the 825 P protection relay with a serial to usb cableusing a non modem cable. When i try to coonect to the unit i keep getting an error code STS 0x2.. Can someone tell me what is the error code is, or what my problem is. [/INST] A USB converter can be used, however, you need to assign it to one of these 4 ports: COM 1, 2, 3 or 4 on the machine. Connect the USB adapter serial port to the 825-P using a standard null-modem cable with the pinout shown in the technote below. Aid 32388 - Connecting to the 825-P through computer serial port using the MPS Explorer Software - fuzzy logic Please remember to Rate the Comments( ) to enhance the reputation of the User who provided help,or close your Topic using the ( ) button over the answer that solved it. Thanks... \\n </s> |
<s>[INST] Motion Instruction MCD ( Motion Change Dynamics ) Do we have to hold rung true in front of this instruction to get it to work correctly? Or do we just one shot it? [/INST] Bruce, take a look to the attached picture... As you see, it executes in one scan normally; anyway it is better to chech the status of .DN bit to make sure everything has gone well.However it is a transitional instruction, so it executes fine with one shot, when rung condition changes from false to true. From RS5000 Ref. Manual Some relay ladder instructions only execute when rung-condition-in toggles from false to true. These are transitional relay ladder instructions. Motion Instruction Reference Manual pagg. 111-117 - fuzzy logic \\n </s> |
<s>[INST] 865 Medium Voltage Differential Feeder Protection Summary: 865 Medium Voltage Differential Feeder ProtectionHi What is the exact part number for 865 Medium Voltage Motor & Feeder Differential Protection? http://ab.rockwellautomation.com/Circuit-and-Load-Protection/Medium-Voltage/865-Medium-Voltage-Protection [/INST] check page 45 of this document http://literature.rockwellautomation.com/idc/groups/literature/documents/br/1503-br010_-en-p.pdf \\n </s> |
<s>[INST] 22- COMM-E and Drive Explorer I have used the 22-comm-e with powerflex40's and never had a problem. THis time I am using powerflex4's with a 22-comm-e and an 22-xcomm base (for housing the 22-comm-e) and I am going use multiple drive mode. Where I am currently stuck is that I cannot get into the 22-comm-e with drive explorer. I gives me some sort of error about text family not recognized. I am using ethernet to access the comm-3 parameters. Any ideas? Is it the x-comm htat's screwing me up? Do I need and add on. It says that I need to set these parameters initial before powering the drives. I just don't get it because I have accessed these before except they were always installed ina drive instead of the 22-xcomm.ANy help is appreciated [/INST] As far as I can remember, you have to follow these steps: 1. Set the 22-COMM to Multi-Drive2. connect to it only one drive3. access the drive (using the embedded HIM) and set the communication parameters (see image below - leave A104 to node 100)4. cycle power to the drive Now, the 22-Comm should be accessible by Drive Explorer. Hope this helps, - fuzzy logic \\n </s> |
<s>[INST] powerflex 753 DPI error I have a powerflex 753 that is getting a DPI error from port 2 the HIM module, this fault causes the drive to shutdown. is there any way to have the drive hold last state and not fault? thank You [/INST] A DPI error from the HIM cannot be ignored, the HIM may be asserting a stop. Make sure you are not using a datalink to modify a parameter that cannot be changed (refer to knowledgebase article 62479). Check the connection between the HIM cradle and the main control board. Try swapping HIM's. Contact free drive tech support at (262) 512-8176. \\n </s> |
<s>[INST] Single phase to Three phase drives for welder application Greetings, Has anyone every done an application involving a 1phase to 3phase drive application to provide power to welding equipment? I just took a call from a customer for 5 such units. Thanks. [/INST] Futher to my question; we are looking at adding a sine wave filter to the output of the drive to provide the cleanest possible power output to the welding machine. Is there anything else that I should be nervous of? Thanks \\n </s> |
<s>[INST] Ultra 100 IPM Thermal Protect Fault not resetting We have several 1398-DDM-019 Ultra 1000 dirves that all simultaniously faulted with IPM Thermal Protect Fault. We cannot reset or clear these faults, even with drives disabled, have re-downloaded configuration via UltraMaster, still faults right away. Is this a blown IPM module? Should I just replace the drives? [/INST] It could be related to AC line noise…. Take a look to the following technotes: Aid 20974 – Aid 21657 (this is referred to Ultra3000, but is the same for Ultra100) Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] Powerflex40P 22-COMM-E Summary: Powerflex 40P unable connect via EthernetI can not connect via Ethernet with Powerflex 40P. I use Drive Explorer 6.04.99-Full, 22-COMM-E. I try to connect and get the message: This is not a supported device. [/INST] Is your Ethernet cable connected to the Ethernet port on the 22-COMM-E or is it plugged into the DSI port on the drive itself? The DSI port LOOKS like an RJ45 port, but is NOT Ethernet. You must be certain you're plugged into the 22-COMM-E port. If you're certain you're correctly connected, have you tried using CCW? It's a free download and provides nearly the same functionality as Drive Explorer. \\n </s> |
<s>[INST] gv 3000 fault code F 3 not F03 any ideas I have a GV3000 where it starts up with F 3, F in the first 7 seg and 3 in the last flashing with every led at the same time.Tech support suggested the 15v rail for encoder... yes that is for a F03 fault. My 15v rail is ok along with all the other rails. No button presses / combination will do anything.A top panel from another larger drive will give me access but starts with the mismatch code for controller / power stage but would allow me to start the matching process but as this belongs to a different drive I cannot spare it.I suspect the memory is corrupted but unable to clear it.Any Ideas?Thanks in anticipationTim Smith [/INST] Did you already try what is suggested in the User Manual ? Attached is a screenshot of the indications.... Hope this helps... - fuzzy logic \\n </s> |
<s>[INST] RSView32 and PowerFlex Drive communication Can RSView32(or other HMI) read/write PowerFlex Drive Parameter without controller over Ethernet/IP? [/INST] Yes, it is possible using PCCC object.... see this technote (35328) where you may find an example made for Panelview Plus (View ME) ... a similar solution could be realized in other HMI software. Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] Powerflex 753 losing Max Fwd Speed after power Reset We are having a powerflex 753 connected to the PLC over ethernet. When we try to change the Max Fwd Speed (P520) from 50Hz(old ) to 70Hz(new) , we found that it takes the setting and motor runs a bit faster , but when we power recycle we see that the Max Fwd speed goes back to 50Hz . The parameter P300 is set to Hz only and not RPM We tried for other parameters and they are getting saved even after restart Any suggestions ?? [/INST] Hi Rahul, Disconnect the drive from the Ethernet communication and change the parameter P520 using keypad. Recycle the power and check, If Drive retain the value, then check the datalinks. If Drive lost the updated value of parameter and return to default value, flash the drive on latest firmware.. \\n </s> |
<s>[INST] Powerflex 700 in Torque mode Anyone have any good examples or know where I can look for running a PF700 in torque mode? Thanks Kevin [/INST] Start, of course, with the User Manual (20B-UM002) and the Reference Manuals (PFLEX-RM001 and PFLEX-RM004). What is your application like ? The PowerFlex drive Application Sets might match what you're doing: http://www.ab.com/drives/drvappsw/ Here's a query to the Literature Website that delivers all the Publications on PowerFlex 700: http://tinyurl.com/ydg9wxe \\n </s> |
<s>[INST] Powerflex 753 speed ramping with Digital Input Hi I am having a PF753 drive with Digital I/O control . Now we need to set the drive to work in following way . When start command is given the drive will run at a minimum speed . When a digital input from selector switch is given then the speed should be ramp up by certain percentage . say for e.g if the start speed is 10hz , when the input is given then it will run at 11hz , and when second time the input comes to drive the drive should run at 12hz , in this way the speed needs to ramp up every time input comes. Is this possible ?? [/INST] P177 - DI MOP Inc Digital Input Motor Operated Potentiometer Increment see p73 and p395 https://literature.rockwellautomation.com/idc/groups/literature/documents/pm/750-pm001_-en-p.pdf \\n </s> |
<s>[INST] PowerFlex 753 fault history Summary: Unable to locate fault history I am trying to locate the fault que in my 753. I am only able to locate the last fault code. [/INST] Ron, comprehensive history of fault information is available through the fault que (via HIM screens and / or software tools such as Drive Explorer). Take a look to the HIM Enhanced User Manual, page 44; you will find instructions about the Viewing/Clearing Drive Faults or Alarms. - fuzzy logic In order to enhance Forum's contributors reputation, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] Competing against ITT PumpSmart / Aquarvar Pump Controllers with PowerFlex Hi there, Has anyone recently been up against ITT PumpSmart or AquaVar Pump Controllers? I have a local (AB friendly) Integrator that is currently up against this product on a job, and I was wonder if anyone could offer me some competitive collateral to offer to my integrator? Any help at all? Thanks. [/INST] nan \\n </s> |
<s>[INST] 1747-SCNR Loses Keeper when Power Cycled. I have read the tech note on the issue with Powerflex 700 drives using a 20-COMM-C module possibly causing keeper loss on a Controlnet scanner. The situation I have is the same condition but occurs on networks with Powerflex 1336 plus 2 drives utilizing scanports and networks with Powerflex 700 drives. When we power down the PLC we get the SIGM message and I/OU displayed. We have to re-download the network file and then everything starts working, The scanner is a 1747-SCNR series A Rev C with four 1336 Plus 2 drives - Catalog 1336F Major Rev 40 Minor Rev 001. I believe these are utilizing scan ports for their comms. The same issue happens to 1747-SCNR Controlnet scanners controlling PowerFlex 700 VC 600V drives utilizing DPI to ControlNet modules, with a mix of drives at Major Rev 3 Minor Rev 002 and Major Rev 4 and Minor Rev 010. How do we avoid the Keeper loss or having to redownload the network after we cycle power to the PLC?? Do we need to flash the drive firmware or is this a scanner issue?? [/INST] The keeper is stored in the lowest numbered ControlNet address of a network. Make sure that the drive is not the lowest number. Also make sure that any redundant processor rack is never the lowest address, it creates a LOT of overhead. Good Luck,Tobin \\n </s> |
<s>[INST] Export Faults and Alarms Log Hi everyone. Is it possible to export the Faults and Alarms Log from the axis propreties ? I my application, I have several Kinetix 5500 for motion control and I would like to export all the Faults and Alarms log from the different axis to create a diagnostic page. Thanks in advance [/INST] Hi, From the help tab in studio 5000 The Faults & Alarms page displays the current status of faults and alarms log structures currently in the controller for this axis. The display is read-only except for the ability to clear logs independently. don't think it is possible I am afraid. \\n </s> |
<s>[INST] 2-phase Powerflex 755? Hi Is it possible to use only two phases (230V each) for supplying Powerflex 755 driving 3-phase motor? I am asking because I've noticed that some of our power inverters are connected to three phases but when I measure current in each phase there is only current in L2 and L3 and no in L1. [/INST] Rockwell technical data document: http://literature.rockwellautomation.com/idc/groups/literature/documents/td/750-td001_-en-p.pdf page 9 says frames 1 through 7 can be supplied with single-phase, at the cost of derating the drive capacity by 50%. You cannot select by software to single-phase the drive, you have to wire it that way. What is the voltage between each of the legs? \\n </s> |
<s>[INST] PowerFlex 755 , High Starting Current Summary: PowerFlex 755 , High Starting CurrentDear all , The problem description :I have a blower on a powerFlex 755 I have a problem with starting the blower , I did many trials . What happened at the beginning that the frequency of the blower was over shooting , for example the setpoint was 15 Hz and it reached 22 Hz and then it came down to 15 , but the current was high . After trying many trials , what is happening now is that the current is high at starting . It looks like that the blower is running faster than the calculation of the frequency drive . I tried to make the starting time longer or shorter , didn’t help . At the beginning the current go up and down several times and then it reaches a peek and then starts to go down to normal current Does anyone have any idea ? [/INST] How is the drive configured? Flux Vector, V/Hz? It sounds like it a PID routine is trying to control the drive. Try putting the drive in V/Hz mode and see what happens when you tell it to start and ramp to a set speed. If it starts in a satisfactory manner in that simple setup, then your PID is trying too hard to control the drive. \\n </s> |
<s>[INST] 1768-M04SE KINETICS 6000 Has anyone ever heard of Kinetics 6000 losing its Home position which happens everyday ???? [/INST] Rodney, take a look to the following technotes, that may help to check the right configuration for your drive homing (KB notes are related to other motion sercos card... but it is the same principle also for your card) Aid 21590Aid 21828Aid 31045 Hope this helps... :smileywink: - fuzzy logic \\n </s> |
<s>[INST] VFD Capacitor Life Summary: Curious about average capacitor life of a drive. Greetings all, I was asked by a customer today, what is the expected shelf life of a typical VFD capacitor. So, not knowing that answer, I turn to all you wonderful folks out here in the VFD world to draw on your experience. M customer's primary concern is how long they should feel comfortable with a spare drive on the shelf before worrying about the capacitor dielectric breaking down. I look forward to seeing all the responses. Thank you. [/INST] Hi I worked in a plant until the start of the year that was installed in around 1996 with hundreds 1336s, we had a few failures of drive capacitors in the first 3 to 5 years but after that I can not remember drive capacitors going, the controller cards are just starting to fail, spare drives in the store always worked. So from this I would say 10 to 15 years. Hope this helps Ian \\n </s> |
<s>[INST] Motion Instruction Error 11 I have a machine that the MASD instructions in ControlLogix are all erroring with 11 as the error code and an extended error code of 0. The machine has been running for several years, however a Kinetix drive was just replaced. The ControlLogix PLC is version 13 and all the drives have firmware version 1.85 or 1.88. Does anybody know what could possibly cause this? [/INST] Error 11 is 'Axis Not Configured' Chances are that you need to look into the property tab of your axis and make the association with the particular hardware. Did you have to change the Kinetix type in the project tree, or was it an exact replacement as is that was just a hardware change? \\n </s> |
<s>[INST] 2094-EN02D-M01-50 experiencing GuardInternalFault Summary: Weird Fault Never Seen and Hard to FInd Documentation On I have a 2094-EN02D-M01-50 amplifier which is part of an RSlogix Version 20 / Kinetix Motion System which is faulting intermittently. The LED on the Amplifier scrolls Safe Fault 01 Internal Hardware 12 while the RSLogix 5000 Software when you open properties of the Axis shows Guard Fault ; Guard Internal Fault ; Immediate Stop . A search of the Logix online Help got me to this gem of data “An Internal Fault has been detected by the Safety Core Hardware. This can includes safety processor faults, interprocessor communications faults, safety power supply faults and gate drive circuitry.” .. While that tells me what the problem might be I cannot find a guide or descriptions for how to troubleshoot this further. I am waiting for a call back from my RA Distributor Tech/Drives Guru, but also hoped someone here had an idea? [/INST] Hi BobLfoot, have you already seen the following: 518884 - 2094 Kinetix 6200, Kinetix 6500: Drive displays Safe Flt 01 Internal Hardware 12 - fuzzy logic In order to enhance the reputation of the Forum's contributors, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] Single VFD PF755 multiple motors, get overcurrent F12 fault Summary: Single VFD PF755 multiple motors, get overcurrent F12 faultMultiple Motor Application Considerations 502708 The article above did not mention how to deal with autotune. Some articles on some forum says do not autotune for the single VFD multiple motor. Then how to deal with autotune options? skip it or set to ready or calculate? We face F12 HwOvercurrent fault when running one drive 2 motors application. We disabled slip compensation like KB says, but the fault still comes up. Any suggestions? Thank you [/INST] my colleague did autotune the drive, with two motors connected, I saw some articles that this will confuse VFD for the motor model is based on one motor only. But how to deal with the autotune options, thank you \\n </s> |
<s>[INST] Power Flex 40P I started with an encoder mounted on the shaft of the motor but due to some mechanical difficulties the value that the encoder was reading had some errors and was unreliable to use for accurate positioning of my Hoist. I then moved the encoder to a direct drive wheel of the hoist and was able to obtain the accuracy that I wanted. A side affect is now that the VFD while in positioning mode attempts to accelerate the drive but while doing so quickly returns to 2 Hz's until it reaches the desired position. I really need it to run at full speed. If someone has seen this issue or knows of a parameter I could adjust to help it compensate I would appreciate feed back. Thanks [/INST] Can you explain positioning mode and what controls the drive to this mode? It sounds like the drive is going to a preset speed depending on input but not knowing any more specifics, input from what? \\n </s> |
<s>[INST] N10:0 File Map to the Power Flex 4M Drive Parameters I'm trying to find the chart that shows how the N10 file with Ethernet Communications maps to the Power Flex 4M drive parameters. Example why is parameter P101 equate to N10:31?What would be the map starts for the other parameter groups, 201, 301, 401? Thanks. [/INST] Welcome to the Forum ! What are you trying to do ?PF4M cannot be directly connected to Ethernet/IP, are you using an external comm module ?Which PLC are you using ?Do you need to change / read parameters or to control the drive ? Please post more details, the more effort you put in writing posts, the more help you may expect to receive... :smileywink: - fuzzy logic \\n </s> |
<s>[INST] Position of output signal shifts when scheduling it with Motion Instruction Hi All , I am scheduling 8 Ouputs using MAOC through 5069 Output module and getting 2 reference inputs to compare with DICAM PLS system. The MAOC is running with virtual axis which has 4ms CUP and geared 2:1 with an CIP axis which has 2ms CUP. I defined the latch and unlatch positions without any additional offset or delay compensation in my output cam editor in order to do simple comparison with command/actual axis position. But the output schedule has not been created in correct position and it shifts with time. As it is seen below , the gearing has too minor error which might not cause such a big difference. For ex. the schedule for output [/INST] Hello srtc could you please give the type of 5069 module that you are using ? a screenshot of the configuration of the 5068 and the MAOC instruction and output cam would be also very helpfull. regards \\n </s> |
<s>[INST] PowerFlex 700 Size 6, Heatsink OvrTemp Summary: Does this drive have fans?Lately we have been encountering the Heatsink OvrTemp fault on our PowerFlex 700 Size 6 drive. If there are fans they are not visible from the anywhere. It started out happing after around 20 minutes of run time and now it happens around 10 to 12 minutes. The heat sink is getting hot and we can cool it with air and the unit runs fine for longer times. I just don't want to pull it apart and not find any fans and we aren't going to spend $15000 to replace this unit just for a couple of fans. Are there Fans on this unit? If so, where are they located? Has anyone attempted to replace their fans? [/INST] Yes, it does have fans. http://literature.rockwellautomation.com/idc/groups/literature/documents/um/20b-um002_-en-p.pdf Fault 8 on page 87 refers to your exact problem. Also look at the technical data document: http://literature.rockwellautomation.com/idc/groups/literature/documents/td/20b-td001_-en-p.pdf There's the installation document: http://literature.rockwellautomation.com/idc/groups/literature/documents/in/20b-in019_-en-p.pdf Unfortunately, Rockwell does not have a service / maintenance manual for PF700, as stated in this article: https://rockwellautomation.custhelp.com/app/answers/detail/a_id/535148 From your description, I would say the fan is no longer spinning. You should check the fan wiring (see the installation document), and verify that it is in fact spinning. They're not quiet; it should be very obvious if the fan is running. \\n </s> |
<s>[INST] PF400 Analog Output not linear with Output Freq. Hi all,I have this problem regarding the linearity of my Analog Output in correspond to the Output Frequency.. this is a Power flex 400, Setting as Follows:Min Freq: 20Hz (parameter 34)Max Freq: 45Hz (Parameter 35)Parameter 82 set to 0 ( VFD analog output req. 0-10V)- Everything is running fine I can command the speed via a third party PLC via 0-10V Analog signal, the commanded voltage is in linearity with the Output Frequency, But the output frequency cannot.. anything I miss out. please help. Gnix [/INST] Looking at the User Manual, if parameter T082 is configured to 0 - OutFreq 0-10, the corresponding minimum output value is 0 volt at 0 Hz. Try to configure it to 21 - MinFreq 0-10 so that your Min Freq corresponds to 0 volts at Analog Out. Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] PF525 Control Module Replacement Summary: Need to replace PF525 Control module with a different HP controllerWe have an issue that we did not have any same size drives in stock to replace a drive with an F110 fault. I was trying to take the parameter from a 10HP 460VAC drive and download to a 1HP 460VAC drive controller. Tried using CCW, handheld HIM and USB utility for PF525. Kept getting errors on the downloads and the parameters would not change from the 1HP settings. Was not able to manually enter the parameters for the 10 HP. The drive is also EthernetIP connected. I saw in various places that the Control module of the PF525s were interchangeable. Is there a procedure to do this update using a different control module from a different size drive? [/INST] nan \\n </s> |
<s>[INST] Powerflex 40 Ethernet/IP Hello! I hope this post is not duplicated, as I have not found any similar. I'm trying to connect a powerflex40 ethernet/ip module to a Fanuc Robot. I'm having troubles because all the manuals I find, there's no setup with the data I need. I have seen that the internal website of the powerflex gives me some information, but not all, such as assembly instances or configuration instance Do I need to have PowerFlex 4-Class HIM ? I don't have it [/INST] Welcome to Engage! Did you already read the EtherNet/IP Adapter User Manual? Appendix C contains a list of EtherNet/IP objects If your robot is an EtherNet/IP scanner, you can find in chapter 4 of the same manual the indications to establish the I/O connection. fuzzy logic Please don't forget to LIKE and highlight the decisive answer: REPLY > Make Best Answer \\n </s> |
<s>[INST] MAM (motion axis move) ERROR Summary: Intermittent MAM.ERI have 2 servo driven linear transfer slides that faults out several times per week. When this happens I have found that the MAM is in ER condition. The only thing that I can find in the vast array of tags is MotionControl[1].ERR = 5. Anyone have any ideas what is causing this. Also, there are 2 of these servo drives and it is happening on either one, but not both at he same time. AXIS_SERVO_DRIVE AMP= 2094-AMP5 MOTOR= MPL-A230P-Vxx2 MotionControl[1].ERR = 5 [/INST] Larsen, you can find more information using the help file with Logix 5000 or Logix Designer. If you go to MAM in the help file, then go near the bottom of the entry, there is SEE ALSO and a hyperlink to Motion Error Codes (.ERR). Click that link to see a table of error codes. Error code 5 is telling you that the MAM instruction is being called before the servo drive has been turned on (it needs an MSO instruction to execute first). One way to prevent this error from occurring is to add a condition making sure that the servo has been turned on. For example, if your axis was called LINEAR_X, then you'd have an XIC instruction checking LINEAR_X.ServoActionStatus. If the ServoActionStatus bit is true, then error 5 will not happen. You should also examine the logic leading to the MAM to make sure that the MSO instruction is getting called properly. Let us know if you need more help. TJ McDermott Systems Interface, Inc. \\n </s> |
<s>[INST] PowerFlex 70 Question Hi All, This is the first time I've been asked this question, and there isn't anything written in the user manual or reference manual that I can find; but are the analog outputs on the PF70 powered from the drive? I want to say yes, but if I have something to back that statement up it would really help. Cheers all. [/INST] Yes, the analog output signals are sourced from the drive's power supply. \\n </s> |
<s>[INST] Set scaling numerator of an axis from PLC Hi all, I need to know if exist a way to set the scaling numerator of an axis via plc. Thanks all. Best regards. [/INST] Hello Nicolosi could you please give us more details. what equipment are you talking about and in which environment Kinetix type ? Motor type ? Studio 5000 version ? do you have a screen shoot ? many thanks regards \\n </s> |
<s>[INST] PowerFlex 40 with Safe Module gives 111 Error Replaced both the drive and Safe Option Module seperately. Still get the error. What else can cause this error? [/INST] Please have a look to the firmware version of your PF40P, version prior to 2.01 could have these problem... If the firmware is ok, then review the following table: Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] 1336S BRF50 Hi there I have got a 1336S-BRF50-AA-EN4-L4 drive and i wish to run it using the inputs from TB3 (L4 option card). I have done a factory reset and have programmed input parameter 12. i have also changed the direction mask to x11111111. But when the try to run it it says Speed at 0.00Hz. The speed is determined by the inpust on TB3 ternimals 26, 27, 28. When I program input mode 12 it automatically sets the maximum freq and voltage to 60Hz and 415Volts and the base freq to 60hz and voltage to 415V as well. Can someone please help me i getting this started please. I need to get it going ASAP! Thanks a lot guys [/INST] It seems your drive is running fine, but the frequency command is 0 Hz, so it stays in run mode at 0 Hz....:smileysurprised:Take a look to the attached screenshot, taken from the User Manual... try to change the Speed Select inputs to obtain a Preset Frequency source, programming some values in Preset Freq. Parameters.For example, all the three inputs closed means use Preset Freq. 7, programming a value of 45 Hz in Preset Freq.7 parameters, the drive should run at that speed. Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] PowerFlex 700H will not acclerate Summary: This drive will not increase the output frequency with a load attachedHere I am with yet another 700H question. We have a PowerFlex 700H, frame size 10, driving a 250hp centrifugal horizontal pump in a Waste Water facility. After the last power up, when called for, the drive will not increase the frequency output with the load attached. If we attempt to run the pump, the display on the HIM indicates accelerating but no increase in the output frequency and no output current. Occasionally you see a flicker of each but not long enough to register much of a value. But, if we disconnect the motor, send a start, the drive will ramp up the correct output frequency with no output current (because there is no load attached). 1)The motor turns freely, 2)The motor is not shorted to ground, 3)The motor does not have an open winding, 4)This happens with control over Ethernet/IP or control locally at the HIM. We have triple checked the drive parameters with an identical drive running next to this one. None have changed. We do NOT get any faults or alarms. I am looking for any input as to what to try or check next. Jason Wirtz Controls Technician Sioux Falls Water Reclamation 4500 N Sycamore Ave Sioux Falls, SD 57104 605-906-1324 [email protected] [/INST] It sounds like your current limit is set to around zero. Please verify parameters 147, 148, and 149. If you can upload a DNO file, we can give you a separate set of eyes on the problem. \\n </s> |
<s>[INST] 700S F43 VoltageFdbk Loss Summary: DC=940V NO FAULT, DC=990V FAULTThe site use Ansaldo rectifier ,and the DC voltage is DC940V. 700S works well(Frame 10 385A) When change to AFE rectifer, and the DC voltage changed to DC990V. 700S generated F43 VoltageFdbk Loss.... Unbelievable!!! Thanks [/INST] nan \\n </s> |
<s>[INST] Servo motor, cable, driver Series A vs Series B Summary: The diffrence between of Series A vs Series B of servo motor, cable, driverHello all, I am confused when I am seeing the name plate of motor, cable, and driver of servo system of Allen-bradley. There are two series A and Series B. And I already tried to search the manual but don't find the answer. Someone, please help me to explain the difference between two series. Really appreciated. Thank you! [/INST] Welcome to the Forum ! When a product maintains the same part number and only the series changes, it reflects changes in manufacturing process and/or parts used in its assembly. These changes maintain or improve the quality and performance of the product and should not affect its performance. In order to understand which differences are between two series of a product, you can try to post specific item codes. Sometimes products of different series are directly replaceable, sometimes not. - fuzzy logic In order to enhance the reputation of the Forum's contributors, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] Power fail on Powerflex 400 Please help with this one as well, same client same powerflex 400 250A unitI am getting really tired of this Power Loss Fault, and the worst part is it does not auto-reset not does it allow me to reset remotely. No, I did NOT experience a dip during operation – the other running drive had no problem. It’s costing us water now at the rate this is going... So it seems the bus volts did drop. A bit strange that other running drive did not also report a fault... why? In any event, WHY does it not auto-reset? Or, alternatively, if this is a fault that does not permit auto-reset then why can I not even reset a Power Loss Fault with the reset input OR with the Fault Clear Parameter (197)? From Subject Received Size Joshua Grimm power loss fault drives 3:33 AM 88 KB [/INST] Did you see Aid 49990 ? There is a known problem with some PF400... maybe you're in that case... A Type 2 fault may require drive or motor repair, or is caused by wiring or programing errors. The cause of the fault must be corrected before the fault can be cleared. Hope this helps - fuzzy logic \\n </s> |
<s>[INST] Motion Axis Properties Catalog Number I'm having trouble finding the Catalog Number for a TLP servo motor in the Axis Properties / Motor Device Specification. Do I need to update a Motion database? Using Logix Designer v33.12 Kinetix 5300 [/INST] I struggled with this very recently. It was a pain to overcome. There are several technotes in the knowledgebase to combat this issue. QA60848 did it for me in the end: https://rockwellautomation.custhelp.com/app/answers/answer_view/a_id/1129466/loc/en_US Basically, there was a newer AOP I had to download and install for the Kinetix 5300. (I was using TLP-B series motors.) Hope this helps, if you have not already figured this out on your own. Regards, RM \\n </s> |
<s>[INST] PF753 drive with safe stop hi I am using a PF753 drive for on of my projects.(20F11GD034AA0NNNNN).The control panel has a E-stop circuit present with a potential free contact. Can i program the TB1-Di2 pin as a Safe stop.Is the safe stop option module 20-750-S1 is necessary for the safe stop to work? [/INST] http://literature.rockwellautomation.com/idc/groups/literature/documents/rm/750-rm001_-en-p.pdf You should read this manual carefully. The short answer is yes, you do need the card if you want a safety function. The digital input you reference can be used as a STOP, but it is not a safety stop. \\n </s> |
<s>[INST] Powerflex 755 Fault on Ethernet error Hello I'm looking for a way to disable ALL drive faults associated with using an embedded Ethernet module with Powerflex 753/755 drives. We will be using hard-wired control, but Ethernet for monitoring purposes. We don't want any Ethernet errors/issues to fault the drive when it's online. I'm currently testing with a PF755 demo setup, and have been unsuccessful in figuring out how to disable those faults. Any help is appreciated. Thank you [/INST] Set Comm Flt Action to something other than fault. Selecting hold last, or zero data should work. PF755, port 13, parameters 54-57 PF753, port of ENETR card, parameters 33-36 \\n </s> |
<s>[INST] Ultra5000 firmware update I have just installed ultraware version 1.82 on my laptop and when I connect to a ultra5000 controller I recieve a message stating that the firmware in the controller is older than the version of ultraware. Can anyone please inform me how to install and where to find the necessary updated firmware. [/INST] Welcome to the Forum ! I'm only aware of the following technote with firmware for U5k: 70783 - Ultra 5000 firmware Latest version is 1.8.1, I don't know if it is enough for your Ultraware version to work... otherwise, I suggest to call Technical Support to get more infos. - fuzzy logic In order to enhance Forum's contributors reputation, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] SERCOS Card inquiry Is the Sercos card supposed to be installed where the Processor is at? or can it be placed in the Remote rack? [/INST] Motion Modules CANNOT be located in remote chassis See Aid 41712 for details. - fuzzy logic \\n </s> |
<s>[INST] Power Flex 700 , VFD failure due input short circuit Summary: VFD failure rate is high. What are possible reason. If failure due to DC bus voltage( 745 V), how can I lower DC bus voltage.We are using Power Flex 700 VFD in crane hoisting application. we have enabled torque proving mode. We are facing problem that failure rate of these drive is very high. On average every 9-12 month VFD power input side ( Rectifier) get shorted and fuse blown up. Our observation is while crane tools lowering DC bus voltage is reaching around 745 Volt. I would like to know. 1. Is due to this DC bus voltage , VFD failure rate is high. 2. How can I control DC bus voltage to lower level. Thanks, Shashi [/INST] 745V bus voltage is normal for a 480V input. If your input voltage is not 480, then yes, 745 bus voltage might not be correct. It would help if you gave specifics - exact drive model number, motor nameplate data, line voltage, design of system - that is, do you have a dynamic braking resistor, brake chopper module, line reactor, load reactor? Have you put a power monitor on the system? \\n </s> |
<s>[INST] Motor Spec - ImportTool2.15.0 - Import doesn't work. Good Morning, I have a problem importing a non-rockwell motor into the motion database. Since several versions of Studio 5000, I can no longer see my motor in the list. However, the import seems to work perfectly. Does anyone have an explanation ? On my old program I can select it but on the new one with K5300, I have to fill it in by hand and there is always a risk of error... Thank you B.R Alex [/INST] You probably need a new cmf file which specifies the motor is compatible with the Kinetix 5300. David \\n </s> |
<s>[INST] IAM Kinetix power size Summary: How to determined the IAM size? I have two questions about the IAM power size. The IAM power size depends from the servomotor size that is connected to the IAM? or, The IAM power size depends from the drives size are connected in the same rack? [/INST] The answer to your question is, BOTH! The best possible way to size Rockwell servo drive products is to download and install Motion Analyser. Give it enough information about the process which you are applying the hardware and you'll get very good and reliable results. One tricky spot is deciding if the multiple axes in the rack will be operating at the same time or in a coordinated manner. Rockwell's default selection for this question is NO, which means the IAM will be sized to the smallest possible load and give an artificially small overall power available. Be careful to set this choice properly so the IAM is sized to the rack properly. This goes towards your second question. If the axes are uncoordinated and do not all operate at the same time, then the individual axis size will likely drive the size of the IAM, (your first question). Proper sizing of this module is a balancing act. It is conceivable that you could end up with an IAM that is rather larger than you need for the individual axis attached to the drive because you need the larger overall power for the entire rack. Does that answer your question adequately? I DO strongly recommend using Motion Analyser. It's a free download and is really quite an excellent software tool. I'm NOT an employee of Rockwell Automation so this is not a sales pitch. \\n </s> |
<s>[INST] PowerFlex 400 Multiple Speed Sources Summary: Want two sources of speed Analog In and a PresetIs it possible to have multiple speed sources for the PowerFlex 400? What I'm trying to accomplish is to have a pump run normally throughout the day with the Analog In signal as the speed source. This is how it works now. Have a selector switch run the pump at max speed for clean up at night. For reference here is what I have: P035 - 80.0 Hz [Max Hz] P036 - 2 [2 Wire Start] P038 - Started out at 2 [Analog In 1], this is where I tried to set it up at 4 [Preset Freq] P039 - 30.0 Sec [Accel Time] P040 - 30.0 Sec [Deccel Time] T051 - 8 [Preset Frequency] T052 - 14 [Anlg1 InCtrl] T069 - 2 (4-20mA) [Analog In 1 Select] A144 - 80.0 Hz [Preset Frequecy 1] I have a switch going from the jumper of 01/11 to 02. This starts the drive. This works as desired. The Analog In for the speed reference is on terminals 13 (+) and 14 (Com). This is the speed reference. This works also as desired. What I tried to do was have a 2 way selector switch with Terminal 04 [Digital Common] on one end and it would either make contact with Terminal 05 [Digital In 1] or Terminal 06 [Digital In 2]. This did not work. The drive wouldn't even move. So I put P038 back to 2, and it worked like it did before. The DIP switch is on SRC... Should I move the wires from Terminal 04 to Terminal 01/11? Is what I'm thinking possible? Thanks. [/INST] I just tested this and answered my own question. Yes the common wire should be from Terminal 01/11 not Terminal 04. I guess this could be helpful for anyone else who may need it. \\n </s> |
<s>[INST] 1394 Serial Cable Part Number Anyone know the part number for a 1394 Serial Cable?Im told it is a straight through DB-9 Male to Female but I can't find a Rockwell part number. [/INST] You are told correct. You just need pins 2,3 & 5 straight through - so you could just make one as well? good luck \\n </s> |
<s>[INST] Moving While Gearing I need consultation about MAM over MAG instruction. My system is combine with 1 virtual axis that run in fix speed, it' s belt coveyor and another axis is film feeding (A-B motor, MPL series and controlled with Kinetix6K). I've problem of deviation of belt conveyor speed that effect to servo speed that run by MAG instruction( belt conveyor is master and servo is slave). After I read Help document on RSLogix5000 in topic that we can put MAM instruction to conpensate the error but in Help document no have any sample code to apply to my system. Could you please recommend me or give me some sample code. Thank you **************************message for Help DocumentMoving While GearingAn incremental MAM instruction may be used for the slave axis (or master axis if the Axis Type is configured as Servo) while the electronic gearing is enabled. This is particularly useful to accomplish phase advance/retard control. The incremental move distance can be used to eliminate any phase error between the master and the slave, or to create an exact non-zero phase relationship. Incremental MAM instruction may also be used in conjunction with electronic gearing to compensate for material slip.Normally a gear ratio of 1 is used with phase adjustment. A 1:1 ratio ensures that the computed phase error does not change before performing the move to correct it. Electronic gearing is not normally used with absolute moves, since the ultimate endpoint is not predictable. To successfully execute a Motion Axis Gear instruction, the targeted axis must be configured as a Servo Axis Type and the axis must be in the Servo On state. If any of these conditions are not met than the instruction errors. [/INST] I believe you are mixing terms. A virtual axis exists only in the control code. It has no real component at all. If you want your film axis slave to follow your belt conveyor, there must be an encoder attached to the belt conveyor. The encoder can be wired into the K6K drive to its aux. encoder input. You would then use this encoder as a servo axis. You cannot issue motion commands, but you can issue home commands to it, and use it as the master axis for MAG. When I create drive trains as you describe, I add a scaling tag to the gear ratio. I would create a tag something like:GEAR_RATIO = MASTER_VALUE/SLAVE_VALUE*SCALING_FACTOR Usually, SCALING_FACTOR is equal to 1.0. A small variation away from 1.0 allows for the physical world (slippage of film, tolerance of drive roller, etc.) without ruining the basic factors. \\n </s> |
<s>[INST] Motion Arm Watch (MAW) I have a piece of equipment that is currently using a MAW instruction to time time a dispensing valve to axis motion. The instruction suggests that the arm is useful for syncing operations to a specified axis position. The position is watched at the servo update rate (very fast) but the the problem is that the logic scan time that is waiting for the WatchEventStatus to be true could be very slow. Is this instruction any better than comparing the .ActualPosition to a certain value. I mean after all, the coarse update rate is the fastest you can expect anything to be read in logic anyways. So why is this instructin even used. The ActualPosition is coming in at the coarse update rate anyways and this is the same time you will see the WatchEventStatus change state as well. I wanted to make sure I understand this instruction and why the original programmer may have used it this way. Thanks in advance for any feedback or advice. [/INST] The MAW would be used to trigger an Event Task. The event task interrupts regular scanning when the MAW triggers and executes the Event task. \\n </s> |
<s>[INST] Scroll the message. I am using Factory Talk View Studio version 12. The message does not fit on the space I have. Is there any way to scroll the message from right to left or vice versa automatically to show the whole message? For example, when it's got the trigger, the message keeps passing to show it all. Is it clear? [/INST] Here are some ideas: 1. Using the existing FTVSE graphic object with variable data. Rather than using a static message, insert a String variable where the String value comes from a String tag in a controller. You can create logic in the controller to scroll your message through the String tag in the controller. The HMI will display the value that it gets from the controller. If the HMI display is updating at once a second, then the scrolling would be rather slow as you would not want the logic to shift the characters faster than the HMI can read them. 2. Rather than using the controller to shift the characters, you could write some VBA to shift the characters in the String variable with the VBA running on the HMI screen. 3. ActiveX control or .NET control.\n </s> |
<s>[INST] MAS that does not work anymore Summary: MAS that does not work anymoreHello, I have 2 machines the same, 1 l306erm automaton in each machine and 2 kinetix 5500 drives in each I develop the program on the first machine, no worries. I import the same program on the second machine it works no worries, Except ... if I turn off the machine. when I restart, the shutdown commands MAS of the 2 dimmers work more. everything else works fine. MSO MAM .. etc .. only MAS stop engine orders that no longer work. If I get the program back into the machine and put it back into the (same) machine, it works again until the machine is turned off. Thanks for your help excuse my english this is an automatic translation. Bonjour, J'ai 2 machines les même, 1 automate l306erm dans chaque machine et 2 variateurs kinetix 5500 dans chaque j'ai développer le programme sur la première machine, pas de soucis. j'importe le même programme sur la deuxième machine cela fonctionne pas de soucis, Sauf ...si j'eteint la machine. lorsque je redémarre , les ordres d’arrêt MAS des 2 variateurs de fonctionne plus. tout le reste fonctionne correctement. MSO MAM .. etc.. uniquement les ordres d’arrêt moteur MAS qui ne fonctionne plus. Si je récupère le programme dans la machine et le réinjecte dans la (même) machine cela fonctionne a nouveaux jusqu’à ce que l'on éteigne la machine. [/INST] I found this subject that corresponds http://forums.rockwellautomation.com/posts/226843cee3 I did not find tech note 41735 \\n </s> |
<s>[INST] Powerflex 525 - Phase loss. I want to ask if this setting “A557 phase loss detection” is parameter that can be used to detect phase loss on 3 phase motor . And if “phase loss treshold” A576 is set good if default is 25% for induction motor . My power supply is 400Volt AC as for Europe , i was wondering if 25% phase loss treshold is good set for this kind of power supply , because american is 460 volt if iam correct. I just need it to do its job and detect the phase loss. I don't currently have a vfd to test it on, that's why I'm asking. [/INST] This parameter is used to monitor the output phases only. If an output is removed, there is a motor wiring issue or the voltage falls below the threshold the drive will trip on F021 Output Ph Loss. 25% of 400 is 100Volts so you would need to lose 300Volts on a phase to trip.\n </s> |
<s>[INST] F4 fault Summary: powerflex 4M series fault F4 hello, anyone ever experienced f4 fault on 4M series ? The manual says plus/minus %10 devitation in supply voltage is acceptable. Measured AC supply voltage with an power quality analyzer and never found values less than 375 V. Wiring is carried out with shielded cable between drive and motor end, shield are connected to gnd as shown in manual. Any suggestions ? thank you [/INST] This problem has not been fixed. There are six drives installed in the same cabinet . Each drive has a an overload breaker on the power input side . the breaker inputs are tied with three phase a copper bus . The incoming three phase from the main cabinet breaker is also connected to breaker inputs. I have seen that when this problem occurs the voltage on the main breaker goes down, but only in this cabinet. There are other cabinet for other machines which do not see any drop in voltage. So the voltage drop is not caused by the network. Somehow voltage is pulled down in the drives cabinet, What might be the reason? I have meggered all the motors and found Ok. Could it be one drive with a defective rectifying circuit or capacitor? \\n </s> |
<s>[INST] PoewrFlex700 HIM Start Problem Dear all, Q1: HIM Start ProblemI had install a Powerflex700 drive with DDC control enable. The Powerlfex700 drive config to run at Auto & Manual Mode, Digital In 1 set as Start Drive & Digital In 3 as AUTO/MANUAL Mode selection. Speed Control by Analog In 1 in 0-10V input. In AUTO mode, VFD was control by DDC via terminal input and the VFD works fine. While in Manual mode, the HIM take control by press ALT-AUTO/MAN, the HIM takeover the VFD control and can start and adjust VFD speed. However, once I push the Stop button(Which is red in color) the drive stop and cannot be start again by press the Start button(Which is green in color). I had to recycle power of the drive in-order to gain the MANUAL mode control again from the HIM. Also I had check that the HIM Stop button(Which is red in color) can stop the VFD in both MANUAL & AUTO mode. Then in-order to regain the VFD control, we had to recycle the VFD power again. Would anyone can help?? What is the problem and is there any config parameter I had to checked with?? Q2: Analog In ProblemOur DDC contractor use johnson control controller and speed control by 0-10V, during the T&C we found that the VFD cannot received the true signal. Actually when the DDC AO output 10V to VFD, we measured the VFD Analog In 1 had read only 7.4V?? Is that the problem of Impedence? Any thing we can do to solve it? Q3: HIM Frequency Display Minus Sign Problem My VFD was configured to run in reverse direction in order to get the Motor Runs in correction direction. Howeve the frequency display in HIM with minus sign and how can I remove it?? Any idea or suggestion?? Thousand thanks for kindly assistance in advanced. [/INST] A1. Please read the note on the bottom of page 1-23Important ; Progamming Inputs for 2 wire control deactivates all HIM Start buttons unless parameter 192, [ save HIM Ref ], bit 1 [ Manual Mode ]=1.This will allow HIM to control Start and Jog.You will need to remove the run input before selecting Manual control. A2. you could adjust the min/ max speed required to match the 0-7.5 signal \\n </s> |
<s>[INST] OPTIX - Where in the PC is the Project Databases stored. Does anyone know where the DB's are stored in the PC running the runtime ? - I thought it would be project folder related , but it seems thats not the case as i have managed to corrupt a DB once or twice experimenting with SQL queries , and when you open a previously saved / older project, the problem of the DB seems to still exist. Id like to copy it and drop it back into the correct place rather than rebuild from an error. [/INST] Assuming we are talking about an embedded database (DataStore), with the DataStore's In memory configuration value set to false, Optix will create an .sqlite database file with the DataStore's Filename configuration value and place it in the Windows user's AppData directory. If you don't have a Filename configured, Optix will create a file with some guid-looking filename. Example path shown below, C:\Users\{username}\AppData\Local\Rockwell Automation\FactoryTalk Optix\Emulator\Projects\{project name}\ApplicationFiles\filename.sqlite. I would also recommend doing an internet search for a DB browser for SQLite. Makes it easy to see the contents of this embedded database. Just don't have it, or try to open when running Optix.\n </s> |
<s>[INST] STEP LOGIC IN DRIVE Summary: HOW TO CONFIGURE DRIVE IN STEP LOGICcan anyone upload a document by which step logic function in Allen Bradley drive can be understood (in easy way)? i have read manuals provided by rockwell but it is very difficult to understand the procedure. thanks. [/INST] Yeah, you are absolutely correct - the step logic as defined in the PF525 manual is as confusing as one can get. I JUST finished programming a 525 for step logic. I suggest, rather than trying to puzzle it out on paper, instead use Connected Components Workbench. Start it up, put a 525 into the project organizer, then go to the wizards tab (or branch of the tree, depending on which version of CCW you're running). In Wizards for this drive, there are two for step logic - one for position and one for velocity. Running the velocity wizard opens a welcome splash screen, with familiar Back/Next buttons at the bottom. Clicking Next takes one to the common settings branch of the wizard. The screen is fairly self-explanatory, you set speed references, accels, and IO configurations necessary for step logic to work. Here, I configured. In my case, I'd configured DigIn TermBlk 05 to be Logic1-In and DigIn TermBlk 06 to be Logic2-In. I set SpeedRef1 for Pot, SpeedRef2 to Step Logic, and SpeedRef3 to Ethernet/IP. Clicking NEXT takes you to Step 0. Step logic always starts with Step 0. Once here, you configure a few things in the ACTION tab (near middle of the window). In my case, Step 0 was a decision branch; I didn't want anything to actually output. I selected NO Output (drive doesn't do anything) Use Accel 1 (meaningless based on the previous setting), and Logic Output state = off. Click over to the Logic tab on Step 0 - this is where the decision branch occurs. There's two decision branches here. You get to go to the next step (step 1) based on what you configure for the first branch. You get to go to some OTHER branch that you can define if different logic is true. In my case, I wanted to go to Step 1 if LOGIC1-IN was true, or go to Step 2 if LOGIC2-IN was true. Step 1, on the Action Tab, I configured direction Rotation Forward, use Accel1, and logic state to be off. I set preset frequency to 5 hz, and also set the time value to 0.1 seconds. Step 1, on the Logic tab, I set Go to Next Step to be NEVER (don't step), and configured the OR choice to be If Time expires and Logic1 is ON, then END-Normal Stop. Step 2, on the action tab, I configured direction Rotation Reverse, Use Accel1, and logic state to be off. I set preset frequency to 5 hz, and also set the time value to 0.1 seconds. Step 2, on the Logic tab, I set Go to Next Step to be NEVER (don't step), and configured the OR choice to be If Time Expires and Logic2 is ON, then END-Normal Stop. That's all that I needed, so Click Finish to close the wizard. If you go to the drive's parameters in CCW, and select the Logic branch in the pull-down, you should see the steps now configured. For whatever reason, the User Manual shows the steps being configured in 4 hexidecimal digits, but CCW displays the step values in binary by default. Dumb choice by Rockwell. Click on the value box for Step 1 and it shows has hex, and you should be able to decode the 4 digits shown by looking at the user manual table for parameters 180-187. CCW makes it far easier to configure step logic than doing it by hand. The logic I outlined above SHOULD make this drive do this: If Input input terminal 5 is activated (by a pushbutton), the drive will run forward at 5 hz for .1 seconds, and then normal stop (not coast). If input terminal 6 is activated (by a pushbutton), the drive will run reverse at 5 hz for .1 seconds, and then normal stop. The drive should index a small distance with each button push. This should allow the operator to bump the drive by the same distance each time without relying on operator dexterity on the buttons. Each bump requires a new button push. The customer's desire is to have crude but accurate positioning capability without the expense of encoder feedback, higher-priced drives, etc. \\n </s> |
<s>[INST] Instruction like BSL. I'm working on a project on Studio 5000, Logix Designer version 32. I'm looking for an instruction that allow me to shift an integer through an array one integer at time. [/INST] It sounds like you want the FIFO Load and Unload, or LIFO Load and Unload instructions: FFL, FFU, LFL, LFU.\n </s> |
<s>[INST] replace pf 753 Hi can i replace power flex 753 frame 1 by power flex 753 frame 2 and power flex 753 frame 2 by power flex 753 frame 1 if yes, i must change program, parameter or not. thank you [/INST] nan \\n </s> |
<s>[INST] 2198-ABQE update channel resolution programatically Hello, first time poster. I have an application using a 2198-ABQE to output encoder positions from K5300 drives to an external system monitoring position. Based on this external systems requirements, they may want to update the output resolution of the 2198-ABQE system dynamically to match their needs. Can I change this setting in the module properties via a SSV or MSG somehow? I cannot find any info on this in the manual. Thanks! edit: I believe I solved my own issue in the module config tags [/INST] Hi @Joseph Theisen and welcome to Engage ! Did your solution work? It would be useful also for other users to have a confirmation... Thanks. fuzzy logic Please don't forget to use the LIKE button and highlight the decisive answer : REPLY > Make Best Answer \\n </s> |
<s>[INST] Ultra3000 E20 fault I have three machines with an Ultra3000 drive using sercos interface. All three machines have very similar design and are less than 2 years old. Two of the three machines have E20 faults intermittently. The newest machine is the one that doesnt fault on E20. I have talked to AB and tried all the likely solutions (changed motor, cables, routing, grounding techniques) but nothing seems to help. We may get rid of it for a while, then it appears out of nowhere again. The two machines that are faulting out are fed from the same 575 V sub, but we do have isolation transformers. The machine that isn't faulting is fed from a different 480 V sub. Just wondering if it is a power/harmonics issue? Has anyone had this issue? [/INST] Just out of curiosity, have you matched the firmware of the newer Ultra 3000 to the older ones? \\n </s> |
<s>[INST] Powerflex 40 - Relay output Summary: Relay output don't stay latchHi, I use a drive PowerFlex 40 and I want to monitor if a fault occur. I'm using 1 of the 2 relays ouput. I use the NO and the commun terminal. If the drive trip, the NO contact only click for around 10 ms. I can't monitor this alarm if the relay doesn't latch for longer. I start the drive with a 2 wire using a relay to start and stop. Is there something else to do ? I tried to modified the parameter A055 and i set it to 0, 2, 4 or 7 and i did trip the motor and i got the fault F007 (Motor Overload). The relay only pulse one shot for a short time. Is there anything that i need to do ? I don't use any timer or any other input of the drive. Thank you [/INST] Is parameter A100 (fault clear) being toggled over a network? Is parameter A092 (Auto Restart Tries) set to a non-zero value? \\n </s> |
<s>[INST] VPL Motor ATEX Hi , can we use some VPL motor in Zone ( ATEX ) ? or do we have any Motor lin which we can use in Zone ? This information is difficult to find , may be because we have not ... [/INST] stephane, Rockwell Automation does not offer a VPL motor with an ATEX rating, but our Technology Partner, Elwood Gettys, offers motors that do. Their website is Elwood High Performance Motors: Servo and Stepper Motors and you can find a list of their ATEX certified motors at https://www.elwood.com/sx.html. They will work with you to find a motor that is compatible with your system and meets your needs. \\n </s> |
<s>[INST] Connected Components Workbench VS RSNetWorx for Ethernet Summary: Why doesn't CCW have some of the features of RsNetWorx 1. I cannot view the Parameters of the Powerflex 523 on RsNetworx for Ethernet. I only have tabs for General, Device Usage, EDS File, and Connections Received. Am I missing something here? 2. CCW does everything I need it to as far as commissioning the VFD and viewing the Parameters but only one at a time. Why can't I Load all drives on the network at once? Why can't I Upload the Parameters for all devices in my project at once (like RsNetworx)? I have 52 VFD's in my control panel. [/INST] Welcome to the Forum ! 1. RSNetworx for Ethernet/IP should not be used to configure device's parameters... it isn't exactly the same tool as RSNetworx for DeviceNet. 2. I've not an answer on that, maybe a future feature ? - fuzzy logic In order to enhance the reputation of the Forum's contributors, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] Powerflex 40 Why wont my acce/dec changes work? [/INST] Welcome to the Forum ! It would be nice to have a more detailed description of your issue... number of the changed parameters, PF40 rating, Motor NP data, description of your tests and results... The more efforts you put in writing posts, the more help you may expect to receive... - fuzzy logic \\n </s> |
<s>[INST] 1336 drive Please , I have AC drive 1336 plus 2 , and we missing the password for login , is there a master password for 1336 plus 2 , or what your recommendation to solve this problem.Thanks [/INST] Call in Rockwell Automation Technical Support for your Region, they will help you to bypass the drive password without resetting all the parameters to factory default. Please be aware the suggested method or infos you will get from them should not be posted here (although many users may well know it ! :smileytongue: ) Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] Powerflex 755 low torque on first run Hi everyone, We have ten 150Hp motors on a lineshaft with one speed master and nine torque slaves. All drives are in FV After power down, the motor torques on the drives are very high and drives fault with over current (I think that's the message) If we accelerate very slowly, we can get the machine up to around 16Hz where something magic happens and the torques drop down to normal Nothing changes on the machine at this point All subsequent runs are fine until power down, then we have the same situation again All drives auto-tuned, but the resulting parameters are incorrect: P621 (slip) 26.5 rpm, but nameplate says 37 rpm P75 (Flux current) 85A, but measured when running OK is 126A Getting the customer to try these parameters to see if the situation improves Anything else we should be looking at? Thanks, Brian [/INST] Hi Brian, you may also try to disable the flux regulator (Parameter 103: Flux Reg Enable for PowerFlex755). The correct settings of the flux current and slip speed are very important to produce torque properly. \\n </s> |
<s>[INST] Kinetix 6000 Line Interface Module I have a case where I need to add a second Kenetix 6000 rack in the same panel as an existing Kinetix 6000. I am not finding specific information regarding whether the Line Interface Module (2094-BL02) can be used for both racks (providing I stay within the current limitations of the unit) [/INST] The 2094 Line Interface Module was originally intended for use with single-rack Kinetix 6000 Multi-Axis servo drive systems; however, application requirements have expanded this limitation to allow for use with multiple parallel AC/DC power loads.See Aid 33313 for details... this is intended to be used with 2094-AL75S, 2094-BL75S, 2094-XL75S-C2, 2094-XL75S-C1 BE AWARE :Do not use 2094-AL09 or 2094-BL02 to drive multiple loads in parallel. This equipment is not designed with built-in short circuit protection.Also, the built-in AC filter does not satisfy CE compliance for parallel loads. - fuzzy logic \\n </s> |
<s>[INST] Self Sensing - Ultra5000 Hello, I have an Ultra5000 drive (2098-IPD-20) and I need it to drive a Moog AC servo motor. The Moog had a resolver so we put a quadrature encoder instead (A+, A-, B+,B-, I+,I-) and wanted to use the self sensing ability of the Ultra500 to automatically determine the commutation. No matter what I define in the drive I keep getting error 39. The motor STARTS rotating and after a couple of seconds it faults out putting error 39. I really don't know what's the problem....? The motor parameters are properly defined and I do see in the Ultraware the encoder counting when I rotate the shaft manually. Any ideas? Thanks,Dan [/INST] Anybody? Dan \\n </s> |
<s>[INST] Is it possible to share JUST a drive file with CCW without making a project file and then an archive file? In CCW, It would be very, very useful to be able to make something like a .DNO file like DriveExectutive does. Currently, one has to create a project, add a drive to the project, be sure to upload from a drive, save the project, then create an archive of it to make a single file that is shareable with other engineers. I'd like very much to be able to save a DNO style file quickly, easily, and reliably. [/INST] TJ, I know this is a very real question and a great example of what we could expect from other users. At this point we need to work on getting these types of feature requests into the business unit at the appropriate level. What's your expectation of such questions? \\n </s> |
<s>[INST] DriveExecutive can not add peripheral on offline status,version5.06.03 Step1:I created a new drive with PowerFlex 753; Step2:All parameters can be seen; Step3:I want to add an expand I/O card(20-750-2262C) through Tab Peripheral ,and click Add...; Step4:Select Port 4,and click OK. Step5:New window is opened,but this window is frozen,not respond for a long time; Step6:Close this window, error message come out HRESULT Code:0x800706be,the remote procedure call failed [/INST] I have find the reason why DriveExecutive have error happen and stay long time while add Peripheral. It is because my hard disk has very small space,less than 1G. I have tried serveral computer with big disk space, this function can be launch normally. \\n </s> |
<s>[INST] Kinetix 300 Is there a way to reset the drive to factory defaults? [/INST] Hello, Kindly find the attached file. Best regards...... \\n </s> |
<s>[INST] PowerFlex 70 Parameter 53 PowerFlex 70 Drive, parameter 53 resets to 3 instead of default 0. Could not find anything in the logic to tell the drive to reset to 3. Has anyone had a similar problem and figured out a solution. Tried the live chat, but nobody's home in the drive department. [/INST] Hmmm... did you already try to Reset the drive to default (P. 197) ? Other useful infos: PF is a Standard or EC version ?Firmware version?Is it connected to a PLC via network card ? Which ?Did you Load parameters from previously saved User Set ? - fuzzy logic \\n </s> |
<s>[INST] Bulletin 160 to PF 525 Conversion Summary: Is there a guide for converting from an older drive? I have several Bulletin 160 drives that communicate over DeviceNet. I'd like to replace these with the PowerFlex 525 using the adapter plate. My question is on converting the ControlLogix program and the mapping. Is there a guide that would show how to remap all the DeviceNet tags, or is this something that would have to be done differently for each application? [/INST] You can download the publication pflex-ap010a-en-p here from Rockwell's Literature Library: http://search.rockwellautomation.com/search?q=pflex-ap010&client=literature&filter=0&ie=UTF-8&oe=UTF-8&output=xml_no_dtd&proxystylesheet=literature&site=literature&getfields=*&lang=en&hl=en&num=20&requiredfields=xlanguage%3AMU%7Cxlanguage%3AEN The main issue is the configuration of the input and output assemblies for the Bul 160. If they were configured as 103 on the input and output side like the 1305 and 1336 Plus drives then the bits line up fairly well. The speed referenced and speed feedback have to be scaled accordingly. See chapter 3. If the 160 used other assemblies then there will be more work to be done. \\n </s> |
<s>[INST] What is the pin-out layout and description for the Kinetix power rails of the DC bus ? Summary: Where can I find out the document for the power rail DC bus pin out define? I can get result of the Upper two pin are DC+, next pins are PE, next pins are DC-, but I do not know what is the meaning of Dear, What is the pin-out layout and description for the Kinetix power rails of the DC bus ? Where can I find out the document for the power rail DC bus pin out define? I can get result of the Upper two pin are DC+, next pins are PE, next pins are DC-, but I do not know what is the meaning of the next pins. my email address is [email protected]. Thanks! | {} DC+ {} DC+ | | {} PE {} PE | | {} DC- {} DC- | {} ?? | {} ?? | ============================================================= _509493 - What is the pin-out layout and description for the Kinetix power rails used for the 2000, 6000, 6200 and 6500? Access Level: Everyone Date Created: 10/15/2012 11:35 AM Last Updated: 03/06/2013 02:26 AM Question What is the pin-out layout and description for the Kinetix power rails used for the 2000, 6000, 6200 and 6500? Answer The pin-outs are the same function 4 x 3 pin-out is: J1 K1 N1 S1 J2 K2 N2 S2 J3 K3 N3 S3 J1 is CAN Hi J2 is CAN Lo The drives all communicate from IAM to AM and back through CAN for items such as converter DC power, faults and status. J3 is SID_Bit 0 K1 is SID_Bit 1 K2 is SID_Bit 2 K3 is SID_Bit 3 S3 is VCC These pins are system identification inputs along with the Vcc give the IAM the ability to read what axis modules are in what slots to determine if single wide or double wide AM. For SERCOS, the IAM assigns the AM SERCOS node addresses. For CIP, Logix assigns the IP but then the System ID should check. Slot filler and shunt modules are unassigned a node address. The slot filler basically completes the Sys Ok string to indicate nothing in that slot. The shunt module is configured in Logix with the IAM shunt regulator. N1 is Sys Ok In N2 is Sys Ok Out This is a series string from IAM to AM back to ensure all of the slots are filled and communicating. This is one criterion that needs to be filled for the contactor enable to be closed. N3 is GShunt Pos S1 is GShunt Neg These are the +/- signals from the IAM converter, which controls the dc bus, and the global shunt command to turn all transistors in the Kinetix products on and off at the same time. This minimizes any fighting of one transistor not in synchronization with another. [/INST] Should be as indicated below. - fuzzy logic In order to enhance the reputation of the Forum's contributors, please rate the replies you got and remember to close the thread clicking Choose as Best Answer button over the solving answer. Thanks ! \\n </s> |
<s>[INST] SMC Flex - displays At Speed but no rotation Summary: When start is sent, it sounds like it is starting and displays At Speed but the motor doesn't spin and it shows its only drawing 4 ampsWhen start is sent, it sounds like it is starting and displays At Speed but the motor doesn't spin and it shows its only drawing 4 amps. 480 VAC, usually draws around 200 amps when running. There are two faults in the fault queue, but I am not sure they are related: [/INST] Has this SMC Flex been running for some time and suddenly stopped working correctly, or is this a new installation and you're in the middle of commissioning? If it's been running for some time, is it controlled from a PLC? Has PLC coding changed such that a stop command is being sent to the SMC Flex? Is there voltage on all three output phases when it's running? Do you have a clamp meter to independently measure output current on each output phase? Check this tech note and in the user manual (link to the manual is in the technote): https://rockwellautomation.custhelp.com/app/answers/answer_view/a_id/545305/loc/en_US \\n </s> |
<s>[INST] Update Cam profile when running I need to update a CAM profile for a motor, without stopping it or disabling the MAPC instruction. The need is to change the ratio between the master and slave motors. Thank you for your help. [/INST] It seems not possible... take a look to Aid 43326 - fuzzy logic \\n </s> |
<s>[INST] PF40 protection device I have an existing Sq. D bucket with breaker that I want to feed a new PF40 drive. Is there anyway to use the existing breaker, if sized correctly? Or will my best option be to feed a J class fuseholder from the existing breaker? Thanks in Advance. Rick Miell [/INST] The PF40 can be installed with either input fuses or an input circuit breaker. Refer to User Manual pages 1-8 and 1-9 and Appendix A for details. Hope this helps… - fuzzy logic \\n </s> |
<s>[INST] Customer Release Date for Engage? I recently promoted Engage on our Global Technical Community call and was asked when the site will be opened for customers. Is there an official date that I can share? [/INST] Hi Michelle. Thanks for the question! While the community is live already, our formal launch of it will happen in the last week of February. Prior to the formal public launch, we will be communicating via Sales Enabler and other communications opportunities internally throughout the month of February. Edited to add: The community is already available to customers. They just need to click engage.rockwellautomation.com to join. If they are not already on SSO /My Rockwell, they will be prompted to create an account. I hope this helps! Let me know if you have any follow-up questions. Thanks, Eileen \\n </s> |
<s>[INST] Powerflex 525 and 753 two sets of variable speeds Hi, this is my first post on here so please be gentle! I have a machine that we perform size changes on and the drives (powerflex 525 and 753) speeds are controlled by linear potentiometer, currently at a size change we change the minimum and maximum frequency settings to give us the speed range required. I would like to add a two position switch to change the frequency's for two different sizes. With the 753 am I correct at thinking I can use parameters 547, 548, 552 and 553 to allow this? I cannot see similar parameters on the 525 so could I use the jog facility to achieve this by having one range of frequency's when in run and a different range in jog and would they both work on the 0-10v potentiometer? Or is there an easier/better way to achieve this? Thanks in advance for any advice. [/INST] Hello, you are very welcome. There are some technical notes available from the Rockwell Knowledgebase that could help with the task ahead. For example for the PowerFlex 753 drive PowerFlex 753: Configuring 2 preset speeds using 1 Digital input can be useful. For the PowerFlex 525 drive PowerFlex 520 series drive: Using Different Preset Speed Values with 2 Wire Control can also help. Both papers above assume the frequency to be switching between fixed values (preset frequencies) stored on parameters on the drive. This could be an easy way to do it. \\n </s> |
<s>[INST] Powerflex 753 displays shows no voltage output or speed feedback in rpms or hz in torque mode min... Summary: replaced a PF700 that showed speed and voltage in torque modewe replaced a old PF700 that went bad. upgraded with a PF753. we no longer can see speed feedback in rpms or hz or voltage output in torque mode. this application is used as a nip roll in a paper machine wet end. we see it running, showing 30 amps output. it shows -0.75 hz with the arrow negative on the HIM. it has a pot for torque reference . it has a positive torque reference. machine seems ok but just wondering. the PF700 used to show speed and voltage output. Is it ok or do we still have a problem. we used to run at 78% torque reference but now only at 28%. if we turn up the torque pot to what we ran at before it trips on overload. [/INST] here is a drive observer picture what we see, estimated rpm about 1400 \\n </s> |
<s>[INST] Resetting Ownership every time when changing Servo motor. Hello, We are using a test panel with servo drives Kinetix 5700 to test several servomotors, but every time I change the unit to test I need to reset the ownership, I'm wondering if is possible to do this without going every time to the Module properties ans pressing the button to reset the ownership? Thanks! [/INST] Reset Ownership operation cannot be executed programmatically, the only way of doing this is manually. fuzzy logic Please don't forget to use the LIKE button and highlight the decisive answer : REPLY > Make Best Answer \\n </s> |